G-BNNA
G-BWGS
Thanks
What Happened to These?
What Happened to These?
Canon 800D & Sigma 150-600 C
Dudley, West Midlands
Shows I'm Attending in 2020:
Well Um..
Dudley, West Midlands
Shows I'm Attending in 2020:
Well Um..
- Dan O'Hagan
- Posts: 2279
- Joined: Wed 13 Apr 2016, 6:05 pm
Re: What Happened to These?
There's this amazing new thing called Google...
- Pen Pusher
- Posts: 7138
- Joined: Sun 31 Aug 2008, 6:34 pm
- Location: St Ives, Cambs
Re: What Happened to These?
Dan O'Hagan wrote:There's this amazing new thing called Google...
And an even more amazing thing called GINFO...
https://publicapps.caa.co.uk/modalappli ... px?appid=1
Brian
Re: What Happened to These?
Aviationcafe wrote:ColeTheDemolisher wrote:G-BNNA
De-registered in JulyColeTheDemolisher wrote:G-BWGS
De-registered in July
what i meant to say was, does anyone have any more information on these?
G-BNNA Destroyed ? how?
Canon 800D & Sigma 150-600 C
Dudley, West Midlands
Shows I'm Attending in 2020:
Well Um..
Dudley, West Midlands
Shows I'm Attending in 2020:
Well Um..
-
- Posts: 312
- Joined: Mon 01 Sep 2008, 12:19 am
Re: What Happened to These?
Dan O'Hagan wrote:There's this amazing new thing called Google...
Jeez. Nothing like a nice friendly response to an innocent query. No wonder this place is like a morgue these days.
Nice one Dan O
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- Posts: 312
- Joined: Mon 01 Sep 2008, 12:19 am
Re: What Happened to These?
Wrt G BNNA, here's the AAIB report on its demise.
All pre-flight checks were completed normally, and the aircraft departed Leicester Airport on a pleasure flight. Having climbed to a safe height, the pilot performed a slow roll and, on completion of the manoeuvre, reduced power to a cruise setting. As he retarded the throttle, the pilot immediately noticed that throttle movement had become stiff and he checked with his passenger in the front seat that she was not impeding throttle movement. Further movement of the throttle failed to clear the problem and the pilot became aware that the engine was now at 1,200 RPM and that he could no longer increase power from the existing setting.
At this stage the aircraft was still within gliding range of Leicester Airport and so the pilot made an emergency PAN call and manoeuvred the aircraft for a forced landing on grass Runway 06. As he positioned the aircraft on final approach the pilot tried to close the throttle completely, but found that this was not possible. As a result of not being able to reduce power, the aircraft was now too high to complete a landing on Runway 06 and the pilot therefore decided to cut the power completely by turning off the magnetos and to land instead on Runway 28. The landing was completed successfully but he was unable to prevent the aircraft from ground looping in the 25 kt crosswind. The aircraft came to a halt having suffered damage to the left main landing gear and the underside of the left wing. The pilot and his passenger, who were both wearing five point harnesses, were uninjured and vacated the aircraft through the normal exits.
All pre-flight checks were completed normally, and the aircraft departed Leicester Airport on a pleasure flight. Having climbed to a safe height, the pilot performed a slow roll and, on completion of the manoeuvre, reduced power to a cruise setting. As he retarded the throttle, the pilot immediately noticed that throttle movement had become stiff and he checked with his passenger in the front seat that she was not impeding throttle movement. Further movement of the throttle failed to clear the problem and the pilot became aware that the engine was now at 1,200 RPM and that he could no longer increase power from the existing setting.
At this stage the aircraft was still within gliding range of Leicester Airport and so the pilot made an emergency PAN call and manoeuvred the aircraft for a forced landing on grass Runway 06. As he positioned the aircraft on final approach the pilot tried to close the throttle completely, but found that this was not possible. As a result of not being able to reduce power, the aircraft was now too high to complete a landing on Runway 06 and the pilot therefore decided to cut the power completely by turning off the magnetos and to land instead on Runway 28. The landing was completed successfully but he was unable to prevent the aircraft from ground looping in the 25 kt crosswind. The aircraft came to a halt having suffered damage to the left main landing gear and the underside of the left wing. The pilot and his passenger, who were both wearing five point harnesses, were uninjured and vacated the aircraft through the normal exits.
Re: What Happened to These?
Found this for G-BNNA, nothing on the other yet. I'll see what I can find.
Mark
https://www.gov.uk/aaib-reports/stolp-s ... april-2003
Mark
https://www.gov.uk/aaib-reports/stolp-s ... april-2003
HTAFC
Re: What Happened to These?
Star Duster G-BNNA by Richard Brown, on Flickr
Both of the posts above are from an incident in 2003 this shot was taken last September at Stoughton and it was very much alive and kicking then.
Both of the posts above are from an incident in 2003 this shot was taken last September at Stoughton and it was very much alive and kicking then.
Rich in Rutland
Re: What Happened to These?
Looking at the photo, I believe the cockpit of G-BNNA is now at the South Yorkshire Aircraft Musueum in Doncaster
Re: What Happened to These?
G-BWGS was still at North Wield in June of this year by the looks of this photo https://flic.kr/p/UPuou9
Rich in Rutland
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Re: What Happened to These?
Think this might answer one of the questions:
https://www.gov.uk/aaib-reports/aaib-investigation-to-starduster-too-sa300-g-bnna
https://www.gov.uk/aaib-reports/aaib-investigation-to-starduster-too-sa300-g-bnna